A4970GLBTR-T Allegro Microsystems Inc, A4970GLBTR-T Datasheet - Page 5

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A4970GLBTR-T

Manufacturer Part Number
A4970GLBTR-T
Description
IC PWM MOTOR DVR FULL 24-SOICW
Manufacturer
Allegro Microsystems Inc

Specifications of A4970GLBTR-T

Lead Free Status / Rohs Status
Lead free / RoHS Compliant

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A4970
PWM CURRENT CONTROL
The A4970 dual bridges drive both windings of a bipolar stepper
motor. Output current is sensed and controlled independently
in each bridge by an external sense resistor, R
comparator, and monostable multivibrator.
When the bridge is turned on, current increases in the motor
winding and it is sensed by the external sense resistor until the
sense voltage, V
input:
The comparator then triggers the monostable, which turns off
the source driver of the bridge.
The actual load current peak will be slightly higher than the
trip point (especially for low-inductance loads) because of the
internal logic and switching delays. This delay, t
μs. After turn-off, the motor current decays, circulating through
the ground-clamp diode and sink transistor. The source driver
off-time (and therefore the magnitude of the current decrease)
is determined by the external RC timing components of the
monostable:
where:
The fi xed off-time should be short enough to keep the current
chopping above the audible range (< 46 μs) and long enough to
properly regulate the current. Because only slow-decay current
control is available, short off times (< 10 μs) require additional
efforts to ensure proper current regulation. Factors that can
negatively affect the ability to properly regulate the current when
using short off times include: higher motor-supply voltage, light
load, and longer than necessary blank time.
When the source driver is re-enabled, the winding current (the
sense voltage) is again allowed to rise to the comparator’s
threshold. This cycle repeats itself, maintaining the average
motor winding current at the desired level.
Loads with high distributed capacitances may result in high turn-
on current peaks. This peak (appearing across R
to trip the comparator, resulting in erroneous current control or
high-frequency oscillations. An external R
be used to further delay the action of the comparator.
The time constant for the delay to produce suitable blank time can
be estimated using:
R
C
T
T
= 20 to 100 kΩ, and
= 100 to 1000 pF.
SENSE
R
C
, reaches the level set at the comparator
I
TRIP
C
C
t
= 0.0114 × R
off
= V
= R
REF
T
C
/10 R
T
T
S
C
C
T
C
C
APPLICATIONS INFORMATION
S
time delay should
S
, internal
) will attempt
d
, is typically 2
This equation assumes that the current control loop duty cycle
is greater than 5% and the voltage on the SENSE pin will reach
99% of the target value set for V
apply to the majority of applications and can be regarded as a
starting value for further optimization by calculation or waveform
measurement.
Depending on load type, many applications will not require these
external components (SENSE connected to E).
Dual Full-Bridge Motor Driver
PWM OUTPUT CURRENT WAVE FORM
V
I
OUT
P HAS E
+
0
LOAD CURRENT PATHS
Bridge On
Source Off, Slow Decay
All Off, Fast Decay
115 Northeast Cutoff
1.508.853.5000; www.allegromicro.com
Allegro MicroSystems, Inc.
Worcester, Massachusetts 01615-0036 U.S.A.
R S
V
BB
SENSE
t
d
. These assumptions will
t
I
off
T R IP
Dwg. WM-003-1A
5

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